Eggshell

A lot of bits of ‘eggshell’ were my thoughts as a pilot from further north handed over his lightweight carbon-fibre cowling for repair.

“Can you fix it?” was his question. The air intake was obviously smashed. Fortunately, he had all the broken pieces, so I’d be able to re-create the original shape. 

The related stress cracks were relatively easy to trace and no problem to fix. 

In addition, the exhaust pipes and muffler had been rubbing on the cowling. We found charred carbon laminate under the ‘heat proof’ shields. So more clearance between hot metal and cowling was required.

“Of course I can,” I replied after quickly running thru the possible repair scenarios in my mind. I was very conscious of the need to do a professional repair restoring strength and flexibility, but with no weight increase. “And fix the exhaust problems at the same time.”

Missing pieces, cracks + rubbing damage
Missing pieces, cracks + rubbing damage
Overheated parts of cowling
Overheated parts of cowling
Pieced-together cowling with widened air outlet
Pieced-together cowling with widened air outlet
Hi-build surface primer
Hi-build surface primer
Sprayed release agent
Sprayed release agent

First task was to carefully re-create the missing air intake shape from all the broken pieces. A bit like gluing a broken eggshell together. Humpty Dumpty all over again. 

To increase the air gap near hot exhaust parts, the air outlet was widened and a strategic ‘bulge’ was added.

This new cowling shape was filled, faired, surface primed, spot-filled, pinhole-filled, etc to get the shape correct and the surface smooth. Then waxed and sprayed with release agent. 

At this stage, I made a temporary fibreglass part-mould of the lower cowling. 

Completed part-mould
Completed part-mould
Part-mould mated with damaged cowling
Part-mould mated with damaged cowling
First carbon layer + patches
First carbon layer + patches
Final carbon layer
Final carbon layer
Re-built cowling (ready for painting)
Re-built cowling (ready for painting)

The lower cowling was cut back and prepped, before the part-mould was mated with it.

I laid-up carbon fabric to create a new air intake, wider air outlet and an exhaust ‘bulge’. Final job was to fill and prime the outside ready for painting.

The rebuilt cowling is as strong and lightweight as the original, but with better exhaust clearance. I even incorporated a sturdier landing light mount.